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2009-141
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Last modified
3/8/2016 11:40:27 AM
Creation date
10/1/2015 3:34:26 AM
Metadata
Fields
Template:
Official Documents
Official Document Type
Change Order
Approved Date
05/19/2009
Control Number
2009-141
Agenda Item Number
12.J.1
Entity Name
Interstate Engineering Corporation
Subject
Change Order No.1 South RO WTP Improvements
Pump Upgrades and MCC Replacements
Area
South RO Plant
Project Number
2008027
Supplemental fields
SmeadsoftID
10644
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Change Order # 1 - South RO Plant Improvements ' <br /> Quotation Descri tionReason for Chane Cost <br /> Replace short 24 " DIP spool with Megaflange adapter to high service <br /> pump suction header, cut and remove concrete pipe trench to allow spool Accelerated corrosion from zinc orhophosphate <br /> injection in <br /> 4R replacement the pipe could cause sudden failure of suction piping to HSP $ 11, 888 . 36 <br /> Replace the two existing 14 " buried gate valves on storage tank effluent <br /> pipes ( owner to furnish 14 " gate valves with actuators ), including Valve actuators are inoperable and require closure <br /> to replace <br /> 7R excavation , compaction , and restoration the 24 " spool $ 10 79L60 <br /> Replace 16 " 316 stainless steel permeate piping, and restore sample lines Corrosion from acid injection has left the <br /> pipe in poor <br /> 8 from permeate header condition, acid leaking on pipe $ 221868 . 31 <br /> Provide temporary location of HSP variable frequency drive to allow full <br /> removal of existing MCC-2, including control wiring and temporary service Failure of MCC-2 has prevented phasing of MCC-2 installation <br /> 10R to VFD and subsequent requirement of the temporary use of VFD $ 8, 286 . 54 <br /> NETA testing of main switchgear, ATS, generator breaker, utility main # 1, <br /> 2, and 6, MCC-3 , and MCP, including infrared survey of contactors; Corrosion in electrical room warrants testing <br />of main <br /> 11 cleaning of corroded equipment listed herein , and test reports to owner components serving plant $ 21 <br />, 978 80 <br /> $ 75 , 813 . 61 <br />
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