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The portion of the scope of services for Work Authorization # 15 dealing with the rehabilitation and <br />reaming of Well No's. 1, 2, 3, and 5 has been completed. These wells were put back into service. The <br />forced removal of the pump and column assembly of well number 4 was completed. The video survey <br />showed that the well was not obstructed and did not require borehole reaming. From inspection of the <br />well, it was determined that the flanged column piping had wom a depression / groove into the wall of the <br />well casing. This depression / groove would not allow the flanged column piping to move out of the well <br />freely. As a result of this, damage to the well occurred rendering it unusable. The damage to Well No. 4 <br />would require attention through a Change Order to Work Authorization # 15 The current expended <br />dollar amount for Work Authorization 15 is $312,520.00. <br />As stated, during normal operation and testing of well numbers 6 and 3, staff discovered that the <br />drawdown measurements for the proper water column height above the pump impellers was not being <br />maintained. The depths of each of the pumps was 40 feet. On June 19, 2001 the Board of County <br />Commissioners approved Work Authorization 18 with CDM in the amount of $83,500.00, for extension <br />of the pump columns 20 feet further down into wells 6 and 3. In addition, Board approval was given to <br />proceed with similar modifications on the other four wells (1, 2, 4, and 5), as part of this same Work <br />Authorization. The current expended dollar amount for Work Authorization 18 is $65,500.00. <br />ANALYSIS <br />As a result of the depression / groove not allowing the column piping from being removed from Well No. <br />4, the pump, discharge head, column assembly, and well casing were damaged. This damage has <br />rendered the current system unusable for production. As explained in the December 12, 2000 agenda <br />item, this damage was anticipated. Staff has investigated the two options of either replacing the complete <br />well and pump system, or repairing it. The estimated replacement cost of the well and pump system is <br />$250,000. The estimated repair cost for the system is $145,440. (See attached draft CDM cost estimate). <br />The less expensive repair option entails making repairs to the damaged well casing, replacement of the <br />discharge head, and re -fitting the well with a compatible capacity pump, with smaller physical <br />dimensions. The smaller physical dimensions of the new pump are needed to allow proper fit, and future <br />removal from the repaired well casing. The largest single item of the repair estimate is for the <br />replacement of the pump assembly, estimated at $55,000.00. This item also has the longest manufacture <br />and delivery time of all the required components to put the pump and well system back in service. Staff <br />has instructed CDM to proceed with placing and expediting the order for the pump. The scheduled <br />delivery date for the pump is March 14, 2002. Staff intends to purchase the pump directly from the <br />manufacturer. <br />Since the forced removal of the pump and column assembly of well number 4, well pump number 6 has <br />experienced mechanical failure. These problems resulted in the pump being removed from the well and <br />re -inspected. The inspection found that several of the bolts that hold the impeller bowls together were <br />missing. These missing bolts may have caused the failure of the pump. Staff has instructed CDM to <br />proceed with rebuilding / repairing the pump and expediting its return to service. Additionally, staff has <br />requested CDM provide a written explanation on the pump failure. The estimated cost for repairs and <br />labor required for restoring the pump to service is $36,000.00. Staff will be seeking reimbursement for <br />these costs as a warranty claim. <br />Concurrently, Well No. 3 has experienced water production problems. Test results on the well are <br />indicating production short -fall from the well. This condition has required removal of the well form <br />service, and the well is currently unavailable for production. At this time the cause of these problems are <br />still being determined. Staff is working very closely with CDM to correct these problems and expedite <br />the return of well number 3 to service. <br />February 12, 2002 <br />60 <br />8! <br />1 <br />06 <br />